XK150 | |||||
Fixed Head Coupe | |||||
Left Hand Drive | |||||
V1029-8 | |||||
1958 | |||||
2004 | |||||
Buxton | |||||
Derbyshire | |||||
Original |
| ||||
Record Creation: Entered on 8 January 2006.
Heritage Notes
Registered: UAS 703
Comments
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2006-01-08 12:37:24 | pauls writes:
Car was at auction in '04
www.practicalclassics.co.uk/auctionlot/by-id/1700374481/
Auction description:
Lot 20: Jaguar XK150 Fixed Head Coupe
An auction of Fine Historic Motor Cars and Automobilia, H&H Classic Auctions Ltd (8th December 2004)
Overview
The 3.4-litre six-cylinder XK engine is reportedly currently in very good order. We understand that the carbs were recently tuned by a retired engineer, who also re-greased the car, made adjustments to the exhaust, set the regulator and generally checked the car out
Lot Details
Auction An auction of Fine Historic Motor Cars and Automobilia
H&H Classic Auctions Ltd, The Pavilion Gardens, Buxton
Type Car
Lot Number 20
Estimate £23000-£25000
Hammer Price £20500
Hammer Price (inc premium) -
Year 1958
Condition rating 2
Registration number UAS 703
Mileage -
Chassis number 5834522BW
Engine number V1029-8
2006-01-15 09:47:23 | pauls writes:
Additional information from H&H auction:
1958 JAGUAR XK150 FIXED HEAD COUPE
RARE AUTOMATIC & FULLY RESTORED
Lot 20
Status SOLD
Estimate £23000 - 25000
Hammer Price £20500.00
Mileage 18500
Colour RED
Trim Colour RED/OATMEAL
Chassis No 5834522BW
Engine No V1029-8
Registration UAS 703
CC 3442
M.O.T APRIL 2005
The rebuild of this 1958-made Jaguar XK150 coupe was commenced in the USA where chassis, running gear, brakes, suspension, carbs and fuel tank were either replaced or renewed or restored to as new condition. Details are in paperwork within the documents file. With all duties paid, the 3.4-litre fixed head was re-imported back to the UK approximately two years ago, being re-registered with the current UAS 703 plates following all completion of all the work.
The vendor tells us that Hartwell of Hereford then carried out a professional conversion from left to right-hand drive and a back to bare metal bare restoration, there being photographs recording this. The three-speed automatic transmission has had the torque converter renewed and is claimed currently to be in very good order. A new wiring loom was professionally fitted, the brightwork either replated or replaced, exhaust renewed in stainless steel, radiator refurbished, dynamo and starter reconditioned, period battery installed, petrol sender renewed and new chromed 16in wires shod with new Avon radials fitted. Some ú3500 alone was spent on a complete interior re-trim by West Midlands specialists Aldridge with static seat belts fitted in the front and twin lap belts in the rear.
The 3.4-litre six-cylinder XK engine is reportedly currently in very good order. We understand that the carbs were recently tuned by a retired engineer, who also re-greased the car, made adjustments to the exhaust, set the regulator and generally checked the car out. A 450 miles round-trip to the Goodwood Festival of Speed was completed without missing a beat. The current MOT will be valid until next April and the tax disc until March.